There is a race between setting up a qgroup rescan worker and completing
a qgroup rescan worker that can lead to callers of the qgroup rescan wait
ioctl to either not wait for the rescan worker to complete or to hang
forever due to missing wake ups. The following diagram shows a sequence
of steps that illustrates the race.
Before the rescan worker started by the task at CPU 3 completes, if
another task calls btrfs_ioctl_quota_rescan(), it will get -EINPROGRESS
because the flag BTRFS_QGROUP_STATUS_FLAG_RESCAN is set at
fs_info->qgroup_flags, which is expected and correct behaviour.
However if other task calls btrfs_ioctl_quota_rescan_wait() before the
rescan worker started by the task at CPU 3 completes, it will return
immediately without waiting for the new rescan worker to complete,
because fs_info->qgroup_rescan_running is set to false by CPU 2.
This race is making test case btrfs/171 (from fstests) to fail often:
btrfs/171 9s ... - output mismatch (see /home/fdmanana/git/hub/xfstests/results//btrfs/171.out.bad)
# --- tests/btrfs/171.out 2018-09-16 21:30:48.505104287 +0100
# +++ /home/fdmanana/git/hub/xfstests/results//btrfs/171.out.bad 2019-09-19 02:01:36.938486039 +0100
# @@ -1,2 +1,3 @@
# QA output created by 171
# +ERROR: quota rescan failed: Operation now in progress
# Silence is golden
# ...
# (Run 'diff -u /home/fdmanana/git/hub/xfstests/tests/btrfs/171.out /home/fdmanana/git/hub/xfstests/results//btrfs/171.out.bad' to see the entire diff)
That is because the test calls the btrfs-progs commands "qgroup quota
rescan -w", "qgroup assign" and "qgroup remove" in a sequence that makes
calls to the rescan start ioctl fail with -EINPROGRESS (note the "btrfs"
commands 'qgroup assign' and 'qgroup remove' often call the rescan start
ioctl after calling the qgroup assign ioctl,
btrfs_ioctl_qgroup_assign()), since previous waits didn't actually wait
for a rescan worker to complete.
Another problem the race can cause is missing wake ups for waiters,
since the call to complete_all() happens outside a critical section and
after clearing the flag BTRFS_QGROUP_STATUS_FLAG_RESCAN. In the sequence
diagram above, if we have a waiter for the first rescan task (executed
by CPU 2), then fs_info->qgroup_rescan_completion.wait is not empty, and
if after the rescan worker clears BTRFS_QGROUP_STATUS_FLAG_RESCAN and
before it calls complete_all() against
fs_info->qgroup_rescan_completion, the task at CPU 3 calls
init_completion() against fs_info->qgroup_rescan_completion which
re-initilizes its wait queue to an empty queue, therefore causing the
rescan worker at CPU 2 to call complete_all() against an empty queue,
never waking up the task waiting for that rescan worker.
Fix this by clearing BTRFS_QGROUP_STATUS_FLAG_RESCAN and setting
fs_info->qgroup_rescan_running to false in the same critical section,
delimited by the mutex fs_info->qgroup_rescan_lock, as well as doing the
call to complete_all() in that same critical section. This gives the
protection needed to avoid rescan wait ioctl callers not waiting for a
running rescan worker and the lost wake ups problem, since setting that
rescan flag and boolean as well as initializing the wait queue is done
already in a critical section delimited by that mutex (at
qgroup_rescan_init()).
Fixes: 57254b6ebce4ce ("Btrfs: add ioctl to wait for qgroup rescan completion") Fixes: d2c609b834d62f ("btrfs: properly track when rescan worker is running") CC: stable@vger.kernel.org # 4.4+ Reviewed-by: Josef Bacik <josef@toxicpanda.com> Signed-off-by: Filipe Manana <fdmanana@suse.com> Signed-off-by: David Sterba <dsterba@suse.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
There may be situations when a server negotiates SMB 2.1
protocol version or higher but responds to a CREATE request
with an oplock rather than a lease.
Currently the client doesn't handle such a case correctly:
when another CREATE comes in the server sends an oplock
break to the initial CREATE and the client doesn't send
an ack back due to a wrong caching level being set (READ
instead of RWH). Missing an oplock break ack makes the
server wait until the break times out which dramatically
increases the latency of the second CREATE.
Fix this by properly detecting oplocks when using SMB 2.1
protocol version and higher.
Cc: <stable@vger.kernel.org> Signed-off-by: Pavel Shilovsky <pshilov@microsoft.com> Signed-off-by: Steve French <stfrench@microsoft.com> Reviewed-by: Ronnie Sahlberg <lsahlber@redhat.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
It should not be larger then the slab max buf size. If user
specifies a larger size, it passes this check and goes
straightly to SMB2_set_info_init performing an insecure memcpy.
Signed-off-by: Murphy Zhou <jencce.kernel@gmail.com> Reviewed-by: Aurelien Aptel <aaptel@suse.com> CC: Stable <stable@vger.kernel.org> Signed-off-by: Steve French <stfrench@microsoft.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The NACKF flag should be cleared in INTRIICNAKI interrupt processing as
description in HW manual.
This issue shows up quickly when PREEMPT_RT is applied and a device is
probed that is not plugged in (like a touchscreen controller). The result
is endless interrupts that halt system boot.
add_early_randomness() is called by hwrng_register() when the
hardware is added. If this hardware and its module are present
at boot, and if there is no data available the boot hangs until
data are available and can't be interrupted.
For instance, in the case of virtio-rng, in some cases the host can be
not able to provide enough entropy for all the guests.
We can have two easy ways to reproduce the problem but they rely on
misconfiguration of the hypervisor or the egd daemon:
- if virtio-rng device is configured to connect to the egd daemon of the
host but when the virtio-rng driver asks for data the daemon is not
connected,
- if virtio-rng device is configured to connect to the egd daemon of the
host but the egd daemon doesn't provide data.
The guest kernel will hang at boot until the virtio-rng driver provides
enough data.
To avoid that, call rng_get_data() in non-blocking mode (wait=0)
from add_early_randomness().
Signed-off-by: Laurent Vivier <lvivier@redhat.com> Fixes: d9e797261933 ("hwrng: add randomness to system from rng...") Cc: <stable@vger.kernel.org> Reviewed-by: Theodore Ts'o <tytso@mit.edu> Signed-off-by: Herbert Xu <herbert@gondor.apana.org.au> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Quoted from
commit 3da40c7b0898 ("ext4: only call ext4_truncate when size <= isize")
" At LSF we decided that if we truncate up from isize we shouldn't trim
fallocated blocks that were fallocated with KEEP_SIZE and are past the
new i_size. This patch fixes ext4 to do this. "
And generic/092 of fstest have covered this case for long time, however
is_quota_modification() didn't adjust based on that rule, so that in
below condition, we will lose to quota block change:
- fallocate blocks beyond EOF
- remount
- truncate(file_path, file_size)
Fix it.
Link: https://lore.kernel.org/r/20190911093650.35329-1-yuchao0@huawei.com Fixes: 3da40c7b0898 ("ext4: only call ext4_truncate when size <= isize") CC: stable@vger.kernel.org Signed-off-by: Chao Yu <yuchao0@huawei.com> Signed-off-by: Jan Kara <jack@suse.cz> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Really enable warning when CONFIG_EXT4_DEBUG is set and fix missing
first argument. This was introduced in commit ff95ec22cd7f ("ext4:
add warning to ext4_convert_unwritten_extents_endio") and splitting
extents inside endio would trigger it.
syzbot found that a thread can stall for minutes inside read_mem() or
write_mem() after that thread was killed by SIGKILL [1]. Reading from
iomem areas of /dev/mem can be slow, depending on the hardware.
While reading 2GB at one read() is legal, delaying termination of killed
thread for minutes is bad. Thus, allow reading/writing /dev/mem and
/dev/kmem to be preemptible and killable.
Theoretically, reading/writing /dev/mem and /dev/kmem can become
"interruptible". But this patch chose "killable". Future patch will make
them "interruptible" so that we can revert to "killable" if some program
regressed.
Currently frame registrations are not purged, even when changing the
interface type. This can lead to potentially weird situations where
frames possibly not allowed on a given interface type remain registered
due to the type switching happening after registration.
The kernel currently relies on userspace apps to actually purge the
registrations themselves, this is not something that the kernel should
rely on.
Add a call to cfg80211_mlme_purge_registrations() to forcefully remove
any registrations left over prior to switching the iftype.
7471fb77ce4d ("md/raid6: Fix anomily when recovering a single device in
RAID6.") avoids rereading P when it can be computed from other members.
However, this misses the chance to re-write the right data to P. This
patch sets R5_ReadError if the re-read fails.
Also, when re-read is skipped, we also missed the chance to reset
rdev->read_errors to 0. It can fail the disk when there are many read
errors on P member disk (other disks don't have read error)
V2: upper layer read request don't read parity/Q data. So there is no
need to consider such situation.
This is Reported-by: kbuild test robot <lkp@intel.com>
Fixes: 7471fb77ce4d ("md/raid6: Fix anomily when recovering a single device in RAID6.") Cc: <stable@vger.kernel.org> #4.4+ Signed-off-by: Xiao Ni <xni@redhat.com> Signed-off-by: Song Liu <songliubraving@fb.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When doing any form of incremental send the parent and the child trees
need to be compared via btrfs_compare_trees. This can result in long
loop chains without ever relinquishing the CPU. This causes softlockup
detector to trigger when comparing trees with a lot of items. Example
report:
At ctree.c:get_old_root(), we are accessing a root's header owner field
after we have freed the respective extent buffer. This results in an
use-after-free that can lead to crashes, and when CONFIG_DEBUG_PAGEALLOC
is set, results in a stack trace like the following:
Fix that by saving the root's header owner field into a local variable
before freeing the root's extent buffer, and then use that local variable
when needed.
Fixes: 30b0463a9394d9 ("Btrfs: fix accessing the root pointer in tree mod log functions") CC: stable@vger.kernel.org # 3.10+ Reviewed-by: Nikolay Borisov <nborisov@suse.com> Reviewed-by: Anand Jain <anand.jain@oracle.com> Signed-off-by: Filipe Manana <fdmanana@suse.com> Reviewed-by: David Sterba <dsterba@suse.com> Signed-off-by: David Sterba <dsterba@suse.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When filtering xattr list for reading, presence of trusted xattr
results in a security audit log. However, if there is other content
no errno will be set, and if there isn't, the errno will be -ENODATA
and not -EPERM as is usually associated with a lack of capability.
The check does not block the request to list the xattrs present.
Switch to ns_capable_noaudit to reflect a more appropriate check.
Tetsuo then noticed that this is because the __memcg_kmem_charge_memcg
fails __GFP_NOFAIL charge when the kmem limit is reached. This is a wrong
behavior because nofail allocations are not allowed to fail. Normal
charge path simply forces the charge even if that means to cross the
limit. Kmem accounting should be doing the same.
Link: http://lkml.kernel.org/r/20190906125608.32129-1-mhocko@kernel.org Signed-off-by: Michal Hocko <mhocko@suse.com> Reported-by: Thomas Lindroth <thomas.lindroth@gmail.com> Debugged-by: Tetsuo Handa <penguin-kernel@i-love.sakura.ne.jp> Cc: Johannes Weiner <hannes@cmpxchg.org> Cc: Vladimir Davydov <vdavydov.dev@gmail.com> Cc: Andrey Ryabinin <aryabinin@virtuozzo.com> Cc: Thomas Lindroth <thomas.lindroth@gmail.com> Cc: Shakeel Butt <shakeelb@google.com> Cc: <stable@vger.kernel.org> Signed-off-by: Andrew Morton <akpm@linux-foundation.org> Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The kernel has no way of knowing when we have finished instantiating
drivers, between deferred probe and systems that build key drivers as
modules we might be doing this long after userspace has booted. This has
always been a bit of an issue with regulator_init_complete since it can
power off hardware that's not had it's driver loaded which can result in
user visible effects, the main case is powering off displays. Practically
speaking it's not been an issue in real systems since most systems that
use the regulator API are embedded and build in key drivers anyway but
with Arm laptops coming on the market it's becoming more of an issue so
let's do something about it.
In the absence of any better idea just defer the powering off for 30s
after late_initcall(), this is obviously a hack but it should mask the
issue for now and it's no more arbitrary than late_initcall() itself.
Ideally we'd have some heuristics to detect if we're on an affected
system and tune or skip the delay appropriately, and there may be some
need for a command line option to be added.
ENOTSUPP is not supposed to be returned to userspace. This was found on an
OpenPower machine, where the RTC does not support set_alarm.
On that system, a clock_nanosleep(CLOCK_REALTIME_ALARM, ...) results in
"524 Unknown error 524"
Replace it with EOPNOTSUPP which results in the expected "95 Operation not
supported" error.
Fixes: 1c6b39ad3f01 (alarmtimers: Return -ENOTSUPP if no RTC device is present) Signed-off-by: Thadeu Lima de Souza Cascardo <cascardo@canonical.com> Signed-off-by: Thomas Gleixner <tglx@linutronix.de> Cc: stable@vger.kernel.org Link: https://lkml.kernel.org/r/20190903171802.28314-1-cascardo@canonical.com Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
This fixes a kernel panic on memcpy when
FORTIFY_SOURCE is enabled.
The initial smp implementation on commit aa7eb2bb4e4a
("arm: zynq: Add smp support")
used memcpy, which worked fine until commit ee333554fed5
("ARM: 8749/1: Kconfig: Add ARCH_HAS_FORTIFY_SOURCE")
enabled overflow checks at runtime, producing a read
overflow panic.
Manually generate the PDPTR reserved bit mask when explicitly loading
PDPTRs. The reserved bits that are being tracked by the MMU reflect the
current paging mode, which is unlikely to be PAE paging in the vast
majority of flows that use load_pdptrs(), e.g. CR0 and CR4 emulation,
__set_sregs(), etc... This can cause KVM to incorrectly signal a bad
PDPTR, or more likely, miss a reserved bit check and subsequently fail
a VM-Enter due to a bad VMCS.GUEST_PDPTR.
Add a one off helper to generate the reserved bits instead of sharing
code across the MMU's calculations and the PDPTR emulation. The PDPTR
reserved bits are basically set in stone, and pushing a helper into
the MMU's calculation adds unnecessary complexity without improving
readability.
Oppurtunistically fix/update the comment for load_pdptrs().
Note, the buggy commit also introduced a deliberate functional change,
"Also remove bit 5-6 from rsvd_bits_mask per latest SDM.", which was
effectively (and correctly) reverted by commit cd9ae5fe47df ("KVM: x86:
Fix page-tables reserved bits"). A bit of SDM archaeology shows that
the SDM from late 2008 had a bug (likely a copy+paste error) where it
listed bits 6:5 as AVL and A for PDPTEs used for 4k entries but reserved
for 2mb entries. I.e. the SDM contradicted itself, and bits 6:5 are and
always have been reserved.
Fixes: 20c466b56168d ("KVM: Use rsvd_bits_mask in load_pdptrs()") Cc: stable@vger.kernel.org Cc: Nadav Amit <nadav.amit@gmail.com> Reported-by: Doug Reiland <doug.reiland@intel.com> Signed-off-by: Sean Christopherson <sean.j.christopherson@intel.com> Reviewed-by: Peter Xu <peterx@redhat.com> Signed-off-by: Paolo Bonzini <pbonzini@redhat.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
x86_emulate_instruction() takes into account ctxt->have_exception flag
during instruction decoding, but in practice this flag is never set in
x86_decode_insn().
Fixes: 6ea6e84309ca ("KVM: x86: inject exceptions produced by x86_decode_insn") Cc: stable@vger.kernel.org Cc: Denis Lunev <den@virtuozzo.com> Cc: Roman Kagan <rkagan@virtuozzo.com> Cc: Denis Plotnikov <dplotnikov@virtuozzo.com> Signed-off-by: Jan Dakinevich <jan.dakinevich@virtuozzo.com> Signed-off-by: Paolo Bonzini <pbonzini@redhat.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
inject_emulated_exception() returns true if and only if nested page
fault happens. However, page fault can come from guest page tables
walk, either nested or not nested. In both cases we should stop an
attempt to read under RIP and give guest to step over its own page
fault handler.
This is also visible when an emulated instruction causes a #GP fault
and the VMware backdoor is enabled. To handle the VMware backdoor,
KVM intercepts #GP faults; with only the next patch applied,
x86_emulate_instruction() injects a #GP but returns EMULATE_FAIL
instead of EMULATE_DONE. EMULATE_FAIL causes handle_exception_nmi()
(or gp_interception() for SVM) to re-inject the original #GP because it
thinks emulation failed due to a non-VMware opcode. This patch prevents
the issue as x86_emulate_instruction() will return EMULATE_DONE after
injecting the #GP.
Fixes: 6ea6e84309ca ("KVM: x86: inject exceptions produced by x86_decode_insn") Cc: stable@vger.kernel.org Cc: Denis Lunev <den@virtuozzo.com> Cc: Roman Kagan <rkagan@virtuozzo.com> Cc: Denis Plotnikov <dplotnikov@virtuozzo.com> Signed-off-by: Jan Dakinevich <jan.dakinevich@virtuozzo.com> Signed-off-by: Paolo Bonzini <pbonzini@redhat.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
The HP Dino PCI controller chip can be used in two variants: as on-board
controller (e.g. in B160L), or on an Add-On card ("Card-Mode") to bridge
PCI components to systems without a PCI bus, e.g. to a HSC/GSC bus. One
such Add-On card is the HP HSC-PCI Card which has one or more DEC Tulip
PCI NIC chips connected to the on-card Dino PCI controller.
Dino in Card-Mode has a big disadvantage: All PCI memory accesses need
to go through the DINO_MEM_DATA register, so Linux drivers will not be
able to use the ioremap() function. Without ioremap() many drivers will
not work, one example is the tulip driver which then simply crashes the
kernel if it tries to access the ports on the HP HSC card.
This patch disables the HP HSC card if it finds one, and as such
fixes the kernel crash on a HP D350/2 machine.
kmsg_dump_get_buffer() is supposed to select all the youngest log
messages which fit into the provided buffer. It determines the correct
start index by using msg_print_text() with a NULL buffer to calculate
the size of each entry. However, when performing the actual writes,
msg_print_text() only writes the entry to the buffer if the written len
is lesser than the size of the buffer. So if the lengths of the
selected youngest log messages happen to precisely fill up the provided
buffer, the last log message is not included.
We don't want to modify msg_print_text() to fill up the buffer and start
returning a length which is equal to the size of the buffer, since
callers of its other users, such as kmsg_dump_get_line(), depend upon
the current behaviour.
Instead, fix kmsg_dump_get_buffer() to compensate for this.
The record logging code looks at the previous record flags in various
ways, and they are all wrong.
You can't use the previous record flags to determine anything about the
next record, because they may simply not be related. In particular, the
reason the previous record was a continuation record may well be exactly
_because_ the new record was printed by a different process, which is
why the previous record was flushed.
So all those games are simply wrong, and make the code hard to
understand (because the code fundamentally cdoes not make sense).
Define the working variables to be unsigned long to be compatible with
for_each_set_bit and change types as needed.
While we are at it remove unused variables from a couple of functions.
This was found because of the following KASAN warning:
==================================================================
BUG: KASAN: stack-out-of-bounds in find_first_bit+0x19/0x70
Read of size 8 at addr ffff888362d778d0 by task kworker/u308:2/1889
2 bytes in MSB of register for clock status is zero during intermediate
state after changing status of sampling clock in models of TASCAM FireWire
series. The duration of this state differs depending on cases. During the
state, it's better to retry reading the register for current status of
the clock.
In current implementation, the intermediate state is checked only when
getting current sampling transmission frequency, then retry reading.
This care is required for the other operations to read the register.
This commit moves the codes of check and retry into helper function
commonly used for operations to read the register.
[CAUSE]
This situation is caused by several factors:
- Fuzzed image
The extent tree of this fs missed one backref for extent tree root.
So we can allocated space from that slot.
- MIXED_BG feature
Super block has MIXED_BG flag.
- No mixed block groups exists
All block groups are just regular ones.
This makes data space_info->block_groups[] contains metadata block
groups. And when we reserve space for data, we can use space in
metadata block group.
Then we hit the following file operations:
- fallocate
We need to allocate data extents.
find_free_extent() choose to use the metadata block to allocate space
from, and choose the space of extent tree root, since its backref is
missing.
This generate one delayed ref head with is_data = 1.
- extent tree update
We need to update extent tree at run_delayed_ref time.
This generate one delayed ref head with is_data = 0, for the same
bytenr of old extent tree root.
Then we trigger the BUG_ON().
[FIX]
The quick fix here is to check block_group->flags before using it.
The problem can only happen for MIXED_GROUPS fs. Regular filesystems
won't have space_info with DATA|METADATA flag, and no way to hit the
bug.
Lenovo ThinkCentre M73 and M93 don't seem to have a proper beep
although the driver tries to probe and set up blindly.
Blacklist these machines for suppressing the beep creation.
The function at issue does not always initialize each byte allocated
for 'b' and can therefore leak uninitialized memory to a USB device in
the call to usb_bulk_msg()
Use kzalloc() instead of kmalloc()
Signed-off-by: Tomas Bortoli <tomasbortoli@gmail.com> Reported-by: syzbot+0522702e9d67142379f1@syzkaller.appspotmail.com Signed-off-by: Sean Young <sean@mess.org> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
This works around a possible stalled packet issue, which may occur due to
clock recovery from the PCH being too slow, when the LAN is transitioning
from K1 at 1G link speed.
This sentinel tells the firmware loading process when to stop.
Reported-and-tested-by: syzbot+98156c174c5a2cad9f8f@syzkaller.appspotmail.com Signed-off-by: Kevin Easton <kevin@guarana.org> Signed-off-by: Kalle Valo <kvalo@codeaurora.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
When switching from any MMC speed mode that requires 1.8v
(HS200, HS400 and HS400ES) to High Speed (HS) mode, the system
ends up configured for SDR12 with a 50MHz clock which is an illegal
mode.
This happens because the SDHCI_CTRL_VDD_180 bit in the
SDHCI_HOST_CONTROL2 register is left set and when this bit is
set, the speed mode is controlled by the SDHCI_CTRL_UHS field
in the SDHCI_HOST_CONTROL2 register. The SDHCI_CTRL_UHS field
will end up being set to 0 (SDR12) by sdhci_set_uhs_signaling()
because there is no UHS mode being set.
The fix is to change sdhci_set_uhs_signaling() to set the
SDHCI_CTRL_UHS field to SDR25 (which is the same as HS) for
any switch to HS mode.
This was found on a new eMMC controller that does strict checking
of the speed mode and the corresponding clock rate. It caused the
switch to HS400 mode to fail because part of the sequence to switch
to HS400 requires a switch from HS200 to HS before going to HS400.
Suggested-by: Adrian Hunter <adrian.hunter@intel.com> Signed-off-by: Al Cooper <alcooperx@gmail.com> Signed-off-by: Ulf Hansson <ulf.hansson@linaro.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
This special case with nbytes=0 is not handled correctly and this
fix now makes sure that -EINVAL is returned when there is en/decrypt
called with 0 bytes to en/decrypt.
Since BUG() and WARN() may use a trap (e.g. UD2 on x86) to
get the address where the BUG() has occurred, kprobes can not
do single-step out-of-line that instruction. So prohibit
probing on such address.
Without this fix, if someone put a kprobe on WARN(), the
kernel will crash with invalid opcode error instead of
outputing warning message, because kernel can not find
correct bug address.
Signed-off-by: Masami Hiramatsu <mhiramat@kernel.org> Acked-by: Steven Rostedt (VMware) <rostedt@goodmis.org> Acked-by: Naveen N. Rao <naveen.n.rao@linux.vnet.ibm.com> Cc: Anil S Keshavamurthy <anil.s.keshavamurthy@intel.com> Cc: David S . Miller <davem@davemloft.net> Cc: Linus Torvalds <torvalds@linux-foundation.org> Cc: Naveen N . Rao <naveen.n.rao@linux.ibm.com> Cc: Peter Zijlstra <peterz@infradead.org> Cc: Steven Rostedt <rostedt@goodmis.org> Cc: Thomas Gleixner <tglx@linutronix.de> Link: https://lkml.kernel.org/r/156750890133.19112.3393666300746167111.stgit@devnote2 Signed-off-by: Ingo Molnar <mingo@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
mdadm run fail with kernel message as follow:
[ 172.986064] md: kicking non-fresh sdb from array!
[ 173.004210] md: kicking non-fresh sdc from array!
[ 173.022383] md/raid1:md1: active with 0 out of 4 mirrors
[ 173.022406] md1: failed to create bitmap (-5)
In fact, when active disk in raid1 array less than one, we
need to return fail in raid1_run().
Reviewed-by: NeilBrown <neilb@suse.de> Signed-off-by: Yufen Yu <yuyufen@huawei.com> Signed-off-by: Song Liu <songliubraving@fb.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
At boot time, the acpi_power_meter driver logs the following error level
message: "Ignoring unsafe software power cap". Having read about it from
a few sources, it seems that the error message can be quite misleading.
While the message can imply that Linux is ignoring the fact that the
system is operating in potentially dangerous conditions, the truth is
the driver found an ACPI_PMC object that supports software power
capping. The driver simply decides not to use it, perhaps because it
doesn't support the object.
The best solution is probably changing the log level from error to warning.
All sources I have found, regarding the error, have downplayed its
significance. There is not much of a reason for it to be on error level,
while causing potential confusions or misinterpretations.
In acpi_pci_irq_enable(), 'entry' is allocated by kzalloc() in
acpi_pci_irq_check_entry() (invoked from acpi_pci_irq_lookup()). However,
it is not deallocated if acpi_pci_irq_valid() returns false, leading to a
memory leak. To fix this issue, free 'entry' before returning 0.
Fixes: e237a5518425 ("x86/ACPI/PCI: Recognize that Interrupt Line 255 means "not connected"") Signed-off-by: Wenwen Wang <wenwen@cs.uga.edu> Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
In cm_write(), 'buf' is allocated through kzalloc(). In the following
execution, if an error occurs, 'buf' is not deallocated, leading to memory
leaks. To fix this issue, free 'buf' before returning the error.
Fixes: 526b4af47f44 ("ACPI: Split out custom_method functionality into an own driver") Signed-off-by: Wenwen Wang <wenwen@cs.uga.edu> Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
Commit aff138bf8e37 ("ARM: dts: exynos: Add TMU nodes regulator supply
for Peach boards") assigned LDO10 to Exynos Thermal Measurement Unit,
but it turned out that it supplies also some other critical parts and
board freezes/crashes when it is turned off.
The mentioned commit made Exynos TMU a consumer of that regulator and in
typical case Exynos TMU driver keeps it enabled from early boot. However
there are such configurations (example is multi_v7_defconfig), in which
some of the regulators are compiled as modules and are not available
from early boot. In such case it may happen that LDO10 is turned off by
regulator core, because it has no consumers yet (in this case consumer
drivers cannot get it, because the supply regulators for it are not yet
available). This in turn causes the board to crash. This patch restores
'always-on' property for the LDO10 regulator.
Fixes: aff138bf8e37 ("ARM: dts: exynos: Add TMU nodes regulator supply for Peach boards") Signed-off-by: Marek Szyprowski <m.szyprowski@samsung.com> Signed-off-by: Krzysztof Kozlowski <krzk@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
because the allocation could fail from iommu_map_page(), and the volume
of this call could be huge which may generate a lot of serial console
output and cosumes all CPUs.
Fix it by silencing the warning in this call site, and there is still a
dev_err() later to notify the failure.
In nvme spec 1.3 there is a definition for data write/read counters
from SMART log, (See section 5.14.1.2):
This value is reported in thousands (i.e., a value of 1
corresponds to 1000 units of 512 bytes read) and is rounded up.
However, in nvme target where value is reported with actual units,
but not thousands of units as the spec requires.
Signed-off-by: Tom Wu <tomwu@mellanox.com> Reviewed-by: Israel Rukshin <israelr@mellanox.com> Reviewed-by: Max Gurtovoy <maxg@mellanox.com> Reviewed-by: Chaitanya Kulkarni <chaitanya.kulkarni@wdc.com> Reviewed-by: Christoph Hellwig <hch@lst.de> Signed-off-by: Sagi Grimberg <sagi@grimberg.me> Signed-off-by: Sasha Levin <sashal@kernel.org>
While the MMUs is disabled, I-cache speculation can result in
instructions being fetched from the PoC. During boot we may patch
instructions (e.g. for alternatives and jump labels), and these may be
dirty at the PoU (and stale at the PoC).
Thus, while the MMU is disabled in the KPTI pagetable fixup code we may
load stale instructions into the I-cache, potentially leading to
subsequent crashes when executing regions of code which have been
modified at runtime.
Similarly to commit:
8ec41987436d566f ("arm64: mm: ensure patched kernel text is fetched from PoU")
... we can invalidate the I-cache after enabling the MMU to prevent such
issues.
The KPTI pagetable fixup code itself should be clean to the PoC per the
boot protocol, so no maintenance is required for this code.
Signed-off-by: Mark Rutland <mark.rutland@arm.com> Cc: Catalin Marinas <catalin.marinas@arm.com> Reviewed-by: James Morse <james.morse@arm.com> Signed-off-by: Will Deacon <will@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
According to the ACPI 6.3 specification, the _PSD method is optional
when using CPPC. The underlying assumption is that each CPU can change
frequency independently from all other CPUs; _PSD is provided to tell
the OS that some processors can NOT do that.
However, the acpi_get_psd() function returns ENODEV if there is no _PSD
method present, or an ACPI error status if an error occurs when evaluating
_PSD, if present. This makes _PSD mandatory when using CPPC, in violation
of the specification, and only on Linux.
This has forced some firmware writers to provide a dummy _PSD, even though
it is irrelevant, but only because Linux requires it; other OSPMs follow
the spec. We really do not want to have OS specific ACPI tables, though.
So, correct acpi_get_psd() so that it does not return an error if there
is no _PSD method present, but does return a failure when the method can
not be executed properly. This allows _PSD to be optional as it should
be.
Signed-off-by: Al Stone <ahs3@redhat.com> Signed-off-by: Rafael J. Wysocki <rafael.j.wysocki@intel.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
[drivers/media/i2c/ov9650.c:706]: (error) Shifting by a negative value is undefined behaviour
[drivers/media/i2c/ov9650.c:707]: (error) Shifting by a negative value is undefined behaviour
[drivers/media/i2c/ov9650.c:721]: (error) Shifting by a negative value is undefined behaviour
Prevent mangling with gains with invalid values.
As pointed by Sylvester, this should never happen in practice,
as min value of V4L2_CID_GAIN control is 16 (gain is always >= 16
and m is always >= 0), but it is too hard for a static analyzer
to get this, as the logic with validates control min/max is
elsewhere inside V4L2 core.
In submit_urbs(), 'cam->sbuf[i].data' is allocated through kmalloc_array().
However, it is not deallocated if the following allocation for urbs fails.
To fix this issue, free 'cam->sbuf[i].data' if usb_alloc_urb() fails.
Signed-off-by: Wenwen Wang <wenwen@cs.uga.edu> Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
If saa7146_register_device() fails, no cleanup is executed, leading to
memory/resource leaks. To fix this issue, perform necessary cleanup work
before returning the error.
Signed-off-by: Wenwen Wang <wenwen@cs.uga.edu> Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
Regulators should be enabled before clocks to avoid h/w hang. This
require change in exynos_bus_probe() to move exynos_bus_parse_of()
after exynos_bus_parent_parse_of() and change in error handling.
Similar change is needed in exynos_bus_exit() where clock should be
disabled before regulators.
This happens because devres_release_all will first remove all the nodes
into a separate todo list so the nested devres_release from
devm_devfreq_unregister_notifier won't find anything.
Fix the warning by calling the non-devm APIS for frequency notification.
Using devm wrappers is not actually useful for a governor anyway: it
relies on the devfreq core to correctly match the GOV_START/GOV_STOP
notifications.
Fixes: 996133119f57 ("PM / devfreq: Add new passive governor") Signed-off-by: Leonard Crestez <leonard.crestez@nxp.com> Acked-by: Chanwoo Choi <cw00.choi@samsung.com> Signed-off-by: MyungJoo Ham <myungjoo.ham@samsung.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
In dvb_create_media_entity(), 'dvbdev->entity' is allocated through
kzalloc(). Then, 'dvbdev->pads' is allocated through kcalloc(). However, if
kcalloc() fails, the allocated 'dvbdev->entity' is not deallocated, leading
to a memory leak bug. To fix this issue, free 'dvbdev->entity' before
returning -ENOMEM.
Signed-off-by: Wenwen Wang <wenwen@cs.uga.edu> Signed-off-by: Sean Young <sean@mess.org> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
Recent changes to the atheros at803x driver caused
ethernet to stop working on this board.
In particular commit 6d4cd041f0af
("net: phy: at803x: disable delay only for RGMII mode")
and commit cd28d1d6e52e
("net: phy: at803x: Disable phy delay for RGMII mode")
fix the AR8031 driver to configure the phy's (RX/TX)
delays as per the 'phy-mode' in the device tree.
This now prevents ethernet from working on this board.
It used to work before those commits, because the
AR8031 comes out of reset with RX delay enabled, and
the at803x driver didn't touch the delay configuration
at all when "rgmii" mode was selected, and because
arch/arm/mach-imx/mach-imx7d.c:ar8031_phy_fixup()
unconditionally enables TX delay.
Since above commits ar8031_phy_fixup() also has no
effect anymore, and the end-result is that all delays
are disabled in the phy, no ethernet.
Update the device tree to restore functionality.
Signed-off-by: André Draszik <git@andred.net> CC: Ilya Ledvich <ilya@compulab.co.il> CC: Igor Grinberg <grinberg@compulab.co.il> CC: Rob Herring <robh+dt@kernel.org> CC: Mark Rutland <mark.rutland@arm.com> CC: Shawn Guo <shawnguo@kernel.org> CC: Sascha Hauer <s.hauer@pengutronix.de> CC: Pengutronix Kernel Team <kernel@pengutronix.de> CC: Fabio Estevam <festevam@gmail.com> CC: NXP Linux Team <linux-imx@nxp.com> CC: devicetree@vger.kernel.org CC: linux-arm-kernel@lists.infradead.org Signed-off-by: Shawn Guo <shawnguo@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
compile-testing this driver on other architectures showed
multiple warnings:
drivers/net/ethernet/nxp/lpc_eth.c: In function 'lpc_eth_drv_probe':
drivers/net/ethernet/nxp/lpc_eth.c:1337:19: warning: format '%d' expects argument of type 'int', but argument 4 has type 'resource_size_t {aka long long unsigned int}' [-Wformat=]
drivers/net/ethernet/nxp/lpc_eth.c:1342:19: warning: format '%x' expects argument of type 'unsigned int', but argument 4 has type 'dma_addr_t {aka long long unsigned int}' [-Wformat=]
Use format strings that work on all architectures.
The streaming state should be set to the first upstream sub-device only,
not everywhere, for a sub-device driver itself knows how to best control
the streaming state of its own upstream sub-devices.
When compile-testing on other architectures, we get lots of warnings
about incorrect format strings, like:
drivers/dma/iop-adma.c: In function 'iop_adma_alloc_slots':
drivers/dma/iop-adma.c:307:6: warning: format '%x' expects argument of type 'unsigned int', but argument 6 has type 'dma_addr_t {aka long long unsigned int}' [-Wformat=]
drivers/dma/iop-adma.c: In function 'iop_adma_prep_dma_memcpy':
>> drivers/dma/iop-adma.c:518:40: warning: format '%u' expects argument of type 'unsigned int', but argument 5 has type 'size_t {aka long unsigned int}' [-Wformat=]
Use %zu for printing size_t as required, and cast the dma_addr_t
arguments to 'u64' for printing with %llx. Ideally this should use
the %pad format string, but that requires an lvalue argument that
doesn't work here.
AER info of PCIe fatal error is not printed in the current driver.
Because APEI driver will panic directly for fatal error, and can't
run to the place of printing AER info.
An example log is as following:
{763}[Hardware Error]: Hardware error from APEI Generic Hardware Error Source: 11
{763}[Hardware Error]: event severity: fatal
{763}[Hardware Error]: Error 0, type: fatal
{763}[Hardware Error]: section_type: PCIe error
{763}[Hardware Error]: port_type: 0, PCIe end point
{763}[Hardware Error]: version: 4.0
{763}[Hardware Error]: command: 0x0000, status: 0x0010
{763}[Hardware Error]: device_id: 0000:82:00.0
{763}[Hardware Error]: slot: 0
{763}[Hardware Error]: secondary_bus: 0x00
{763}[Hardware Error]: vendor_id: 0x8086, device_id: 0x10fb
{763}[Hardware Error]: class_code: 000002
Kernel panic - not syncing: Fatal hardware error!
This issue was imported by the patch, '37448adfc7ce ("aerdrv: Move
cper_print_aer() call out of interrupt context")'. To fix this issue,
this patch adds print of AER info in cper_print_pcie() for fatal error.
Here is the example log after this patch applied:
{24}[Hardware Error]: Hardware error from APEI Generic Hardware Error Source: 10
{24}[Hardware Error]: event severity: fatal
{24}[Hardware Error]: Error 0, type: fatal
{24}[Hardware Error]: section_type: PCIe error
{24}[Hardware Error]: port_type: 0, PCIe end point
{24}[Hardware Error]: version: 4.0
{24}[Hardware Error]: command: 0x0546, status: 0x4010
{24}[Hardware Error]: device_id: 0000:01:00.0
{24}[Hardware Error]: slot: 0
{24}[Hardware Error]: secondary_bus: 0x00
{24}[Hardware Error]: vendor_id: 0x15b3, device_id: 0x1019
{24}[Hardware Error]: class_code: 000002
{24}[Hardware Error]: aer_uncor_status: 0x00040000, aer_uncor_mask: 0x00000000
{24}[Hardware Error]: aer_uncor_severity: 0x00062010
{24}[Hardware Error]: TLP Header: 000000c0010100000000000100000000
Kernel panic - not syncing: Fatal hardware error!
Fixes: 37448adfc7ce ("aerdrv: Move cper_print_aer() call out of interrupt context") Signed-off-by: Xiaofei Tan <tanxiaofei@huawei.com> Reviewed-by: James Morse <james.morse@arm.com>
[ardb: put parens around terms of && operator] Signed-off-by: Ard Biesheuvel <ard.biesheuvel@linaro.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
Then from kernel side, Manage_add invokes the path (add_new_disk ->
validate_super = super_1_validate) to set In_sync flag.
Since In_sync means "device is in_sync with rest of array", and the new
added disk need to resync thread to help the synchronization of data.
And md_reap_sync_thread would call spare_active to set In_sync for the
new added disk finally. So don't set In_sync if array is in frozen.
Signed-off-by: Guoqing Jiang <guoqing.jiang@cloud.ionos.com> Signed-off-by: Song Liu <songliubraving@fb.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
When add one disk to array, the md_reap_sync_thread is responsible
to activate the spare and set In_sync flag for the new member in
spare_active().
But if raid1 has one member disk A, and disk B is added to the array.
Then we offline A before all the datas are synchronized from A to B,
obviously B doesn't have the latest data as A, but B is still marked
with In_sync flag.
So let's not call spare_active under the condition, otherwise B is
still showed with 'U' state which is not correct.
Signed-off-by: Guoqing Jiang <guoqing.jiang@cloud.ionos.com> Signed-off-by: Song Liu <songliubraving@fb.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
The Linux kernel assumes that get_endpoint(alts,0) and
get_endpoint(alts,1) are eachothers feedback endpoints.
To reassure that validity it will test bsynchaddress to comply with that
assumption. But if the bsyncaddress is 0 (invalid), it will flag that as
a wrong assumption and return an error.
Fix: Skip the test if bSynchAddress is 0.
Note: those with a valid bSynchAddress should have a code quirck added.
In build_adc_controls(), there is an if statement on line 773 to check
whether ak->adc_info is NULL:
if (! ak->adc_info ||
! ak->adc_info[mixer_ch].switch_name)
When ak->adc_info is NULL, it is used on line 792:
knew.name = ak->adc_info[mixer_ch].selector_name;
Thus, a possible null-pointer dereference may occur.
To fix this bug, referring to lines 773 and 774, ak->adc_info
and ak->adc_info[mixer_ch].selector_name are checked before being used.
This bug is found by a static analysis tool STCheck written by us.
The last fallback of CORB/RIRB communication error recovery is to turn
on the single command mode, and this last resort usually means that
something is really screwed up. Instead of a normal dev_err(), show
the error more clearly with dev_WARN() with the caller stack trace.
Also, show the bus-reset fallback also as an error, too.
A reboot request sends an IPI via the reboot vector and waits for all other
CPUs to stop. If one or more CPUs are in critical regions with interrupts
disabled then the IPI is not handled on those CPUs and the shutdown hangs
if native_stop_other_cpus() is called with the wait argument set.
Such a situation can happen when one CPU was stopped within a lock held
section and another CPU is trying to acquire that lock with interrupts
disabled. There are other scenarios which can cause such a lockup as well.
In theory the shutdown should be attempted by an NMI IPI after the timeout
period elapsed. Though the wait loop after sending the reboot vector IPI
prevents this. It checks the wait request argument and the timeout. If wait
is set, which is true for sys_reboot() then it won't fall through to the
NMI shutdown method after the timeout period has finished.
This was an oversight when the NMI shutdown mechanism was added to handle
the 'reboot IPI is not working' situation. The mechanism was added to deal
with stuck panic shutdowns, which do not have the wait request set, so the
'wait request' case was probably not considered.
Remove the wait check from the post reboot vector IPI wait loop and enforce
that the wait loop in the NMI fallback path is invoked even if NMI IPIs are
disabled or the registration of the NMI handler fails. That second wait
loop will then hang if not all CPUs shutdown and the wait argument is set.
[ tglx: Avoid the hard to parse line break in the NMI fallback path,
add comments and massage the changelog ]
Fixes: 7d007d21e539 ("x86/reboot: Use NMI to assist in shutting down if IRQ fails") Signed-off-by: Grzegorz Halat <ghalat@redhat.com> Signed-off-by: Thomas Gleixner <tglx@linutronix.de> Cc: Don Zickus <dzickus@redhat.com> Link: https://lkml.kernel.org/r/20190628122813.15500-1-ghalat@redhat.com Signed-off-by: Sasha Levin <sashal@kernel.org>
On !CONFIG_RT_GROUP_SCHED configurations it is currently not possible to
move RT tasks between cgroups to which CPU controller has been attached;
but it is oddly possible to first move tasks around and then make them
RT (setschedule to FIFO/RR).
Also, as Michal noted, it is currently not possible to enable CPU
controller on unified hierarchy with !CONFIG_RT_GROUP_SCHED (if there
are any kernel RT threads in root cgroup, they can't be migrated to the
newly created CPU controller's root in cgroup_update_dfl_csses()).
Existing code comes with a comment saying the "we don't support RT-tasks
being in separate groups". Such comment is however stale and belongs to
pre-RT_GROUP_SCHED times. Also, it doesn't make much sense for
!RT_GROUP_ SCHED configurations, since checks related to RT bandwidth
are not performed at all in these cases.
Make moving RT tasks between CPU controller groups viable by removing
special case check for RT (and DEADLINE) tasks.
Signed-off-by: Juri Lelli <juri.lelli@redhat.com> Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org> Reviewed-by: Michal Koutný <mkoutny@suse.com> Reviewed-by: Daniel Bristot de Oliveira <bristot@redhat.com> Acked-by: Tejun Heo <tj@kernel.org> Cc: Linus Torvalds <torvalds@linux-foundation.org> Cc: Peter Zijlstra <peterz@infradead.org> Cc: Thomas Gleixner <tglx@linutronix.de> Cc: lizefan@huawei.com Cc: longman@redhat.com Cc: luca.abeni@santannapisa.it Cc: rostedt@goodmis.org Link: https://lkml.kernel.org/r/20190719063455.27328-1-juri.lelli@redhat.com Signed-off-by: Ingo Molnar <mingo@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
The load_balance() has a dedicated mecanism to detect when an imbalance
is due to CPU affinity and must be handled at parent level. In this case,
the imbalance field of the parent's sched_group is set.
The description of sg_imbalanced() gives a typical example of two groups
of 4 CPUs each and 4 tasks each with a cpumask covering 1 CPU of the first
group and 3 CPUs of the second group. Something like:
{ 0 1 2 3 } { 4 5 6 7 }
* * * *
But the load_balance fails to fix this UC on my octo cores system
made of 2 clusters of quad cores.
Whereas the load_balance is able to detect that the imbalanced is due to
CPU affinity, it fails to fix it because the imbalance field is cleared
before letting parent level a chance to run. In fact, when the imbalance is
detected, the load_balance reruns without the CPU with pinned tasks. But
there is no other running tasks in the situation described above and
everything looks balanced this time so the imbalance field is immediately
cleared.
The imbalance field should not be cleared if there is no other task to move
when the imbalance is detected.
Signed-off-by: Vincent Guittot <vincent.guittot@linaro.org> Signed-off-by: Peter Zijlstra (Intel) <peterz@infradead.org> Cc: Linus Torvalds <torvalds@linux-foundation.org> Cc: Peter Zijlstra <peterz@infradead.org> Cc: Thomas Gleixner <tglx@linutronix.de> Link: https://lkml.kernel.org/r/1561996022-28829-1-git-send-email-vincent.guittot@linaro.org Signed-off-by: Ingo Molnar <mingo@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
We need to increment the device count atomically before we checkout a
device to make sure that we do not reach the max count, otherwise we get
out-of-bounds errors as reported by syzbot.
Reported-and-tested-by: syzbot+aac8d0d7205f112045d2@syzkaller.appspotmail.com Signed-off-by: Luke Nowakowski-Krijger <lnowakow@eng.ucsd.edu> Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
The call to of_get_child_by_name returns a node pointer with refcount
incremented thus it must be explicitly decremented after the last
usage.
Detected by coccinelle with the following warnings:
drivers/media/platform/exynos4-is/fimc-is.c:813:2-8: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 807, but without a corresponding object release within this function.
drivers/media/platform/exynos4-is/fimc-is.c:870:1-7: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 807, but without a corresponding object release within this function.
drivers/media/platform/exynos4-is/fimc-is.c:885:1-7: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 807, but without a corresponding object release within this function.
drivers/media/platform/exynos4-is/media-dev.c:545:1-7: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 541, but without a corresponding object release within this function.
drivers/media/platform/exynos4-is/media-dev.c:528:1-7: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 499, but without a corresponding object release within this function.
drivers/media/platform/exynos4-is/media-dev.c:534:1-7: ERROR: missing of_node_put; acquired a node pointer with refcount incremented on line 499, but without a corresponding object release within this function.
Signed-off-by: Wen Yang <wen.yang99@zte.com.cn> Signed-off-by: Hans Verkuil <hverkuil-cisco@xs4all.nl> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
When CONFIG_DVB_DIB9000 is disabled, we can still compile code that
now fails to link against dibx000_i2c_set_speed:
drivers/media/usb/dvb-usb/dib0700_devices.o: In function `dib01x0_pmu_update.constprop.7':
dib0700_devices.c:(.text.unlikely+0x1c9c): undefined reference to `dibx000_i2c_set_speed'
The call sites are both through dib01x0_pmu_update(), which gets passed
an 'i2c' pointer from dib9000_get_i2c_master(), which has returned
NULL. Checking this pointer seems to be a good idea anyway, and it avoids
the link failure in most cases.
Sean Young found another case that is not fixed by that, where certain
gcc versions leave an unused function in place that causes the link error,
but adding an explict IS_ENABLED() check also solves this.
Fixes: b7f54910ce01 ("V4L/DVB (4647): Added module for DiB0700 based devices") Signed-off-by: Arnd Bergmann <arnd@arndb.de> Signed-off-by: Sean Young <sean@mess.org> Signed-off-by: Mauro Carvalho Chehab <mchehab+samsung@kernel.org> Signed-off-by: Sasha Levin <sashal@kernel.org>
Firmware files are in ASCII, using 2 hex characters per byte. The
maximum length of a firmware string is therefore
16 (commands) * 2 (bytes per command) * 2 (characters per byte) = 64
Fixes: ff45262a85db ("leds: add new LP5562 LED driver") Signed-off-by: Nick Stoughton <nstoughton@logitech.com> Acked-by: Pavel Machek <pavel@ucw.cz> Signed-off-by: Jacek Anaszewski <jacek.anaszewski@gmail.com> Signed-off-by: Sasha Levin <sashal@kernel.org>
According to the datasheet https://www.ti.com/lit/ds/symlink/lm3632a.pdf
Table 20. VPOS Bias Register Field Descriptions VPOS[5:0]
Sets the Positive Display Bias (LDO) Voltage (50 mV per step)
000000: 4 V
000001: 4.05 V
000010: 4.1 V
....................
011101: 5.45 V
011110: 5.5 V (Default)
011111: 5.55 V
....................
100111: 5.95 V
101000: 6 V
Note: Codes 101001 to 111111 map to 6 V
The LM3632_LDO_VSEL_MAX should be 0b101000 (0x28), so the maximum voltage
can match the datasheet.
which has the hallmarks of a worker queued from interrupt after it was
supposedly cancelled (note the POISON_FREE), and I could not see where
the interrupt would be flushed on shutdown so added the likely suspects.
Bugzilla: https://bugs.freedesktop.org/show_bug.cgi?id=111174 Signed-off-by: Chris Wilson <chris@chris-wilson.co.uk> Signed-off-by: Takashi Iwai <tiwai@suse.de> Signed-off-by: Sasha Levin <sashal@kernel.org>
When creating a raw AF_NFC socket, CAP_NET_RAW needs to be checked
first.
Signed-off-by: Ori Nimron <orinimron123@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When creating a raw AF_IEEE802154 socket, CAP_NET_RAW needs to be
checked first.
Signed-off-by: Ori Nimron <orinimron123@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org> Acked-by: Stefan Schmidt <stefan@datenfreihafen.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When creating a raw AF_AX25 socket, CAP_NET_RAW needs to be checked
first.
Signed-off-by: Ori Nimron <orinimron123@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When creating a raw AF_APPLETALK socket, CAP_NET_RAW needs to be checked
first.
Signed-off-by: Ori Nimron <orinimron123@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
When creating a raw AF_ISDN socket, CAP_NET_RAW needs to be checked
first.
Signed-off-by: Ori Nimron <orinimron123@gmail.com> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
After a reset packet sizes and device mtu can change and need
to be reevaluated to calculate queue sizes.
Malicious devices can set this to zero and we divide by it.
Introduce sanity checking.
Reported-and-tested-by: syzbot+6102c120be558c885f04@syzkaller.appspotmail.com Signed-off-by: Oliver Neukum <oneukum@suse.com> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Endpoints with zero wMaxPacketSize are not usable for transferring
data. Ignore such endpoints when looking for valid in, out and
status pipes, to make the drivers more robust against invalid and
meaningless descriptors.
The wMaxPacketSize of these endpoints are used for memory allocations
and as divisors in many usbnet minidrivers. Avoiding zero is therefore
critical.
Running old skge driver on PowerPC causes checksum errors
because hardware reported 1's complement checksum is in little-endian
byte order.
Reported-by: Benoit <benoit.sansoni@gmail.com> Signed-off-by: Stephen Hemminger <stephen@networkplumber.org> Signed-off-by: David S. Miller <davem@davemloft.net> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>